Friday, March 25, 2011
Saturday, January 8, 2011
Final Fitting, Drilling and Mounting Cockpit Panels – 16 Hours
Saturday, January 1, 2011
Cockpit Aluminum Panels – 8 Hours
This being the first posting of 2011, I would like to first take the opportunity to wish everyone following this blog a happy and prosperous new year.
Installation and fitting of the cockpit panels has been the most challenging so far, so it’s refreshing to think these are the last panels which require fitting prior to the body being fitted.
The splash panels (lower outer, upper outer and transmission filler) have never been fitted or offered up to the frame, unlike the two large cockpit floors and rear firewall which were positioned when the kit exits the factory. The splash panels are a little like jigsaw pieces, however after offering up each panel there is a natural order to how these should be installed.
Interestingly mk3build.com and the Factory Five manual conflict with regard to panel overlap and at this time please don’t take the pictures as an accurate installation as some panels are only shown as a rough orientation to their final position. Later posts will define what I find to be the best orientation.
The initial installation procedure would be to start with both cockpit floors, followed by the panels which cover the X bracing under each door, followed by the rear firewall. The rear firewall may require centering as the temporary positioning at the factory does not necessarily mean this panel is centered.
It will probably take another 10 to 12 hours to finish the final fitting of all the cockpit panels and transmission tunnel cover which will be installed as a removable cover to facilitate maintenance and access to the rear wiring harness.
Tip of the day: Thinking ahead I intend to use bezels were the seatbelt feeds through the firewall, because of this rivet holes were excluded from these areas as the bezels would not fit flush to the firewall due to interference with the rivet heads (see picture).
Wednesday, December 29, 2010
Cockpit Sheet Metal and Filler Patches – 3 Hours
30 Minute Engine Run
During the 30 minute session the engine was exercised through a number of RPM ranges as the FAST system continued its adaptive learning. Temperatures and oil pressures remained stable and at this time no coolant leaks have been identified.
The exhaust tone is just awesome.
Wednesday, December 22, 2010
Day 365 of Build – First Engine Start
Step 3 remove radiator cap so that the coolant system could be “burped”
At this point the excitement is intense, and as you can see from the video the engine actually started on the first attempt and initial gauges checks all looked good.
At 190 degrees the thermostat opened, this quickly leveled the engine temperature at 184 degrees for the rest of the initial testing. Note: the water temperature gauge supplied is in degrees Celsius, 184F is approximately 82C.
Oil pressure at 850 RPM was a constant 55psi dropping to 40psi at higher RPM’s, the voltage remained at a steady 14 volts, fuel pressure is set at 43psi.
The engine was run through a heat cycle of approximately 30 minutes. This will be repeated over the next few days to check for leaks created from heat cycles and to continue the EFI adaptive learning process.
Overall a smooth and successful first start, and a great early Christmas present.
Sunday, December 19, 2010
Vapor Canister & Odd’s and End’s – 4 hours
Vapor lines were run from the gas tank breather and rear axle breather into the canister. The purpose of the canister is to filter gasoline and oil odors as the vapor passes through the charcoal filter.
Lastly today the clutch cable supplied from Factory Five was replaced with an original Ford OEM cable, if you recall in an earlier block it was suggested that an original cable needed less leg pressure to operate. I am pleased to confirm that this is the case, for some reason there is no binding or resistance with an original cable.
Saturday, December 18, 2010
Flexible Fuel Hose – 4 Hours
Normally I am not one for gadgets, over the years I have happily ripped up my hands forcing braided hose into a AN fitting, but no more. I came across this great gadget from Koul Tool, the video explains all. After making three complete hoses today I have to say it is as easy to use as the video suggests.
Tip of the day: A great way to cut braided hose is to mount 2 hacksaw blades, one with teeth forward the other with teeth backwards, this cuts in both directions and significantly reduces fraying of the braid.
Sunday, December 5, 2010
FAST EFI Computer – 2 Hours
Exhaust Hanger & Wiper Motor – 3 Hours
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With both exhausts parallel to the chassis and ground the exhaust hangers were mounted, these provide additional support to the exhaust pipe, and reduce potential vibration stress fractures at the header.
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